Hmmm.... Not sure why the original post is gone :confused:
Recently I purchased a 91' 318i with 150k. The previous owner was very upfront and said he believed the head gasket was bad.
After getting the head off, I quickly realized that the head was infact cracked. Luckily however, I had a spare M42 head.
Taking both heads to the machine shop, here is the list of what was done:
- The valves where used off the E36 M42 head vs. the E30 M42 head's 7mm valve stems. (Thats 12g PER VALVE of weight savings)
-Even with the lighter valves, I used the dual spring setup off of the E30 M42 head. (even tested against the conical s52 springs, they were stiffer!)
- .020" was shaved off of the head for a little better compression.
- I had some minor port work done. (Mostly bowl blending and smoothing everything out)
- Lastly, once I had it up and running again, I threw in a Mark D. tune.
Here is the car as it sits today:

Here is one of the intake ports after port work:

And finally, here is the dyno graph from today (~40 degrees out)

I am happy with the power, considering its a stock motor with minor touches. Having that been said, I have full access to a dyno and would love to move some power up top.
I am open to all suggestions, and I will dyno test them!