Alrighty, I am basically done with the retrofit now. All I need to do is paint the bottom housing & little socket thingy.
I was pulling the pictures off of my camera and came across some from my last business trip to China that I had forgotten about. My last day there was spent in Hong Kong and it was the last weekend of the Dragon Boat Festival.

My hotel room had a pretty sweet view of HK Harbor. HK is easily my favorite city in the world (NYC'ers forgive me!). I rarely go there for business, aside from passing-through, but I have been there for vacation a couple of times. My fiancee speaks Cantonese, so it's nice when we go since I have my own personal "tour guide" lol. Her dad lives & runs a business there, so we basically get to stay for free.

Anyway, time for more car-nerd stuff.
I wanted to use the three stock mounting points (two screw slots on the fender, rubber nub thingy down on the frame rail). The screws were already taken care of, so I went to work getting things working with the rubber nub.

I had some 1.25" black nylon rod stock laying around, so I stuck it in the lathe and did my best to duplicate the cup geometry found in the stock air box. I put the thing into a vise and eyeballed an angle, and then used the mill to cut one end at an angle so that it would sit tangent to the box bottom.

It is held in place by two screws, from the inside of the box. The nylon part had M6 thread inserts installed because...well, plastic threads...you know.

How does it fit? Well, not too bad really. With everything just sitting there, the MAF is only 5mm off, which is not an issue at all since the rubber boot has probably 20mm of flex in it before I would start worrying about stressing it.

I stuffed on an ugly old rubber coupling and everything is great!

Here's my little creation, happily sitting on the nub.

I wanted to get a better fit between the curved housing and the flat face on the cup. So I wrapped the housing in saran wrap, gooped a bunch of plastic-weld epoxy onto the cup and then screwed it all together for a few hours.

After it had a couple of days to cure, I started cleaning it up on the lathe.

The epoxy actually cuts pretty well, if you are using a low enough feed rate. I had the lathe set to 0.0011" per revolution which worked perfectly. No chipping! A super sharp tool also helps.

So here it is, all cleaned up.

Assembled...just needs a little paint.
