Thank you,everyone.
I found this site,read up,like a good Libra.
Sure as poop,I pulled the pan this afternoon.
91 318i,140K,bone stock,run hard,serviced very
well,as I am a mechanic by trade.
One bolt in the pan.
THREE of remaining five are finger loose,or tight,
depending on your attitude.
Two center ones,tight as a drum.
The one dropped bolt was trying very hard to
chew thru the soft steel cone of the scavange pipe.
Good thing it was stuck under it.
Pick up bolts were undertorqued,so I did em all.
11NM with a tiny bit more twisted into the wrench.
I felt the tight ones,they were at that level of tight.
So,I duplicated it as well as I could.
So relieved. I really did not want to look into it,for
I knew the possiblility existed of parts and chunks
laying there,as well.
Spotless,otherwise.
CIA analyst owned it from new,so I was lucky a
persnickity type had it serviced very well.
Thank you ,everyone.
Steve Wilson
Kuztown,Pennsyltucky
P.S. I used the old gasket. I know everyone frowns on this,
but the surfaces were perfect and the gasket was clean.
I used the VW waterpump sealant. I have found this stuff,
dealer sourced,works superbly on everything I have used it on.
Put the thinnest coat possible,perfect seal.
Man,what a relief.