Alllllllllllright! I just got my car back together yesterday, pretty excited. It was down for 3 weeks thanks to some sheisty powder-coating guys. Took them 3 weeks to powdercoat my intake and valve-cover.
Anyway, I took care of the mess under the intake. I changed my 2-3" of fuel line, because it literally fell apart in my hands. I removed the heater plate, and capped the coolant lines between the head and the plastic coolant "junction." I doubled up on the caps, and will update if I experience any problems with them. Changed the vacuum lines, but I still need to get some stronger hoes for my ICV, I believe it is collapsing. Just need to tighten up a few things.
I also removed my fan, and I must say, it's quite nice. The engine stays up between shifts, and seems to transition more smoothly.
I changed my injectors to mustang, 4 pintle injectors. I installed new spark plugs, and converted to the COP kit from the turbo m42 guy.. installed very easily and is a very nice addition.
Just have to install my electric fan, and it'll be ready to ride.
Just want to say, I had to REALLY flush my coolant. I was hydrolocked at the head, and had too much air built up. I had to literally fill and re-fill my coolant lines and massage them in order to get all of the air out. It seems to be running fine right now, but just in case anyone encounters this same problem, try massaging passenger side coolant (when the engine is cold.) and filling with coolant, as this will circulate the coolant.
I'll post pics shortly!