Daily Driver had 380,000 miles on it. No compression on more than one cylinder in 2011. Stored until a couple months ago. Had the Motor apart since 2011. Machined for a stock build. Used Maxsil 2nd oversize pistons, stock cams. Just want to make it a reliable daily again.
Refreshed fuel lines starting with the tank. Suspension is e30M springs over bilstein sports with trimmed bumpstops. New lemforder arms, eyeball mounts, 5series engine mounts, e21 trans mounts, all new 10.9/12.9 fasteners for subframes and or engine. AKG rear street bushing kit, RTAB's delrin w/ 1/2" grade 8 hardware (had to reem holes and make nice fit)
It runs nicely, but as I posted in another thread should of used permatex on the lower timing case to the block. Gasket leaks at the seam. Should never use double gaskets, just one or none. I'll be taking off the head and redoing this after a bit more break in.