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Messages - Rhino

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Engine + Driveline / Loud noise that disappears at high rpm.
« on: July 13, 2008, 02:26:30 AM »
The previous owner told me he replaced the chain recently so i didnt bother changing any of it. the guides from the top looked to be fine.

2
Engine + Driveline / Loud noise that disappears at high rpm.
« on: July 13, 2008, 12:32:28 AM »
I have a loud noise in my engine. IT sounds like a diesel. It is quite discerning. I rebuilt the head and then the sound came. It goes away when i rev the engine above 3500 rpm.

Rhino

3
Engine + Driveline / Overheating and a bad noise!
« on: June 22, 2008, 10:16:35 PM »
I am going to try and reseat it today. and i do like the fix on the bleeder but to be safe i will replace the radator tomarrow and bleed the system, then i will let you all know how it went

4
Engine + Driveline / Overheating and a bad noise!
« on: June 22, 2008, 02:25:16 PM »
I know, but it was running all the way up to the 3/4 mark before i shut it down
it was getting to hot.

5
Engine + Driveline / Overheating and a bad noise!
« on: June 22, 2008, 06:46:19 AM »
If it was a cracked head, it wouldnt of made that drive in a 100 degree weather without over heating.

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Engine + Driveline / Overheating and a bad noise!
« on: June 21, 2008, 07:48:36 PM »
Ok, I bought a e30 318. I knew it had a bad head gasket. The car over heated and had bubbles coming through the expansion tank. So i had the head resurfaced and put on a new headgasket. I did the job on a budget.

After getting the job completely done i started it and the motor has a very loud knocking or Clattering sound. Above 3000rpm it goes away and the motor sounds really smooth. I have 20-50 castrol motor oil in it. I check timing and it seemed ok. i cant figure out the sound. it wasnt there before i did the work.




I drove the car for the first time a good distance in 100 degree weather about 5-8 miles. It stayed just a tick over the 1/4 mark on the temp gauge. Today its the same weather maybe a bit cooler and it started to over heat when sitting at a light. When moving the temp goes down. I let it almost get to the 3/4 mark. Then i shut it down and then i let it cool down. I am just running water. I opened the system to bleed it and the screw broke off. so this is what i used in place of it. I opened the cap and it was bubble but i am pretty sure it was just boiling because i just shut it off.

Any help would be great. I am so frstrated with this car. I am used to working on m30/m20 motors and really need this car to work. I am with out a car for work or school. Feel free to call me if you would like to talk ideas on fixing this. My name is ryan. MY phone number is 408-476-4780.

THANK YOU ALL.

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